South Texas 97
GOLD Star
PO had a Holley Carb model 2300 with a 140 jet? It looked pretty rough and well abused. Truck ran, but a lot of fuel in the carb. Took the carb off and removed the float bowl and the intermediate body where the idle mix screws are. All the screws had damaged heads, too small a screw driver or too much force applied. Replaced gaskets and little washers around the bolts, dunked everything in carb cleaner. Replaced needle valve for the float, the o-ring was crusty, replaced that. And when I took the float bowl off one little brass Venturi thing just fell out.
The idle adjustment screws were missing one o-ring and the remaining one was hard as a rock.
Put it all back together and on the truck, and it pretty much started right up once I set the float level correctly
The idle adjustment screws were missing one o-ring and the remaining one was hard as a rock.
Put it all back together and on the truck, and it pretty much started right up once I set the float level correctly