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- #81
So the thing that took my 40 off the road was a cooked wire and I glossed over that in my last post. The Red/Black wire from my ignition switch sizzled and smoked when I tried to start it to get back to work when I was out for lunch (warm, had not been sitting for a long time). I tried to replace the bad section of wire hoping that could get me going again but I realized quickly that would not work. I need to pull the harness and do this right.
Pulling the harness has been more challenging than I expected due to the fact this is 50 years old and much of it looks like it has never been touched. It also is not easy for a big guy with big hands and long arms to snake them in up behind the dash. This is not really a glamorous thing to photograph but here are a few. The flash makes the rust look worse.
While I do not think the voltage regulator was the issue, I will be replacing it because I simply cannot get the screws out without trashing it. This looks to be the correct one. I am also replacing a few other bits that just did not look good when I was in there.
Getting the dash out was tricky and makes me wonder how I am ever going to get this back together. I will throw in some LEDs while I have it out
You can see where the PO spliced in power for a stereo. While I have everything out I may upgrade or replace the fuse block. I do not expect to be running a fridge or crazy lights so close to stock works for me.
This is the ignition switch that came with the vehicle and was clearly not Toyota. The blue wire was my attempt to see if only that short section was cooked. Noting happened when I tried to start it (probably for the best)
I bought this dash mount Toyota ignition switch which fits like a glove. Any reason why I couldn't use it if I rewire for the blade terminals?
This has taken me much longer than I hoped and I am working in less than ideal conditions. Heater box is out of the way, switches are all disconnected. Most of the harness is out and the rest is just resting there disconnected. I am finding the wire colors on the diagram above are not mating on my 11/69 build date. I am labeling things as I go before I lay it out on a white board hence why I did not rush to get it out... at least now things are close to where they came from vs the harness wrapped up in a ball. Once it is out of the vehicle I can move it to a better lit and warmer spot to work on (and photograph for Mud.)
To be continued....
Pulling the harness has been more challenging than I expected due to the fact this is 50 years old and much of it looks like it has never been touched. It also is not easy for a big guy with big hands and long arms to snake them in up behind the dash. This is not really a glamorous thing to photograph but here are a few. The flash makes the rust look worse.
While I do not think the voltage regulator was the issue, I will be replacing it because I simply cannot get the screws out without trashing it. This looks to be the correct one. I am also replacing a few other bits that just did not look good when I was in there.
Getting the dash out was tricky and makes me wonder how I am ever going to get this back together. I will throw in some LEDs while I have it out
You can see where the PO spliced in power for a stereo. While I have everything out I may upgrade or replace the fuse block. I do not expect to be running a fridge or crazy lights so close to stock works for me.
This is the ignition switch that came with the vehicle and was clearly not Toyota. The blue wire was my attempt to see if only that short section was cooked. Noting happened when I tried to start it (probably for the best)
I bought this dash mount Toyota ignition switch which fits like a glove. Any reason why I couldn't use it if I rewire for the blade terminals?
This has taken me much longer than I hoped and I am working in less than ideal conditions. Heater box is out of the way, switches are all disconnected. Most of the harness is out and the rest is just resting there disconnected. I am finding the wire colors on the diagram above are not mating on my 11/69 build date. I am labeling things as I go before I lay it out on a white board hence why I did not rush to get it out... at least now things are close to where they came from vs the harness wrapped up in a ball. Once it is out of the vehicle I can move it to a better lit and warmer spot to work on (and photograph for Mud.)
To be continued....