I pulled the drive train out to final weld the mounts, fix up the floor, weld in the cross member and do a few other things that are easier while it is out. After doing all this I reinstalled the drivetrain. This pic was taken during the reinstall:
This is a flex a lite 180 3300 cfm electric fan. I chose to go this way because the stock mech fan left no room to plumb the intake to the DS, combined with my slightly higher mounted engine with a taller truck manifold, while using dual batteries on the PS. The rad mounting bracket is original FJ, although I moved the rad down about 1 inch in the bracket and moved it forward 1 inch by drilling new holes in the bracket mounts. This shift forward was possible because I reworked my grill to take up less space back at post 65. Both of these adjustments were necessary to leave room for the fan and allow the hood to close now that the rad is further forward. I was back and forth about using the ECU to control the fan but it is not programmed in at the moment so the flex a lite controller will have to do.
The exhaust is done back to the muffler, I painted the welds with VHS flame proof paint. Probably a waste of time but it takes attention away from my poor exhaust pipe welding. I used band clamps in 2 spots so I should be able to remove it down the road without cutting. I spent a little time wrapping select wiring with heat shield tape. You can also see the crossmember and scab plates in this pic.
Here is the final resting place of the drivetrain, it is mounted at about 4 degrees down at the back:
To shift the 4L60e I chose a black B & M Magnum Pro Stick. I will modify the cable linkage mount a little to move it away from the exhaust. The plan is to build a enter console to mount the shifter, 80 series e brake handle, CB and possibly an auxiliary heater.
The steering shaft mod is complete too, it was simply redoing it and having the upper u joint right after the steady bearing on the firewall. This gave enough clearance to us the C6 manifolds with their heat shields. I forgot to take a pic before I reinstalled the intake, but if you look close in the second pic below you can see the shaft and u joint.
THE PAYOFF: 6 or 7 weeks ago I pulled the 1.5F, today I was able to drive my LS powered 43 around the block for the first time seated on a tool box. I’m sure it is not a record speed swap but I’m pretty happy none the less. The drive was cut short because of my failed attempt to use a 3 piece lower rad hose which leaked everywhere and I have not wired the fan up yet. I’m going to order one of those flashy rad hoses from summit.
This is how it looked after it’s maiden LS powered trip, sans front bumper/winch: