Alright. As promised here is my update. I had been away in Mexico for a bit but after I got back I was able to get some time in. I took the pistons, rods, and crankshaft to a performance shop near me to check the balance. They spun the crank up and it was in good balance, the pistons were also good. They did have to do a bit of work on the rods though, they were about 16 grams out. Hindsight is 20/20, if I were to do it again I would buy myself a good quality scale, check the pistons, and balance the rods myself like RockDoc did. I don't think it would be too hard. Also, I know I said I wasn't going to but I ended up using the ARP rod bolts. The main reason is because I have this crazy idea in the back of my mind about maybe wanting to mildly turbo this thing in the future. So I did it as insurance, and hey, it can't hurt. I modified the head of the bolts myself. Here is the high tech jig I made for grinding the bolts with a belt sander,
I figured out what geometry I needed and ground down to that. I also made sure I took the exact same amount of material off of each bolt by checking the weight after grinding. After I had them all ground I tested them in the block and they all clear the camshaft nicely.
My first step was to clean the block and head really well. I cleaned the oil galleys and coolant passages, thread chased all the holes, chamfered the head bolt holes in the block, and installed the core plugs.
I then got the crank bolted in, the pistons and rods assembled, rings on, and bolted the rods to the crank. The ring and bearing clearances were all in spec. Bolted on the timing plate with the torx screws, pressed the brand new oem cam gear on the reground camshaft and installed it. Those clearances were all good as well. I then installed the oil pump but discovered that the crankshaft was hitting part of the bracket that supports the 3fe oil pickup tube. Also after bolting the oil pump in I double checked that the distributor slid in and out nicely.
I ground off the tab on each side and now the crank turns with plenty of room.
I then messed around with the oil pan for a bit. The rod bolts were hitting in three spots with the pan bolted up with no gasket. The rods were still touching a bit even after grinding the pan as much as I was comfortable. After inspecting the situation I noticed that each nut that was hitting had the tip of the hex pointing at the pan. So I turned those a bit so the flats of the nut were facing the pan and voila! No more tapping. Double checked after the pan was bolted up with the gasket and it seems good. Tapped and plugged the oil galley in the head, bolted it on and torqued to spec, lifters, push-rods, and rocker assembly installed, pushrod cover, timing cover, and crank pulley installed. Started working on mounting the accessories. I also bought some uhmw rod to make a body lift out of.
My next step is to get some hardware to bolt the new oem water pump on with (my 2f didn't come with one) and then secure the ac and alternator brackets on properly. I am still figuring it out but since I have the earlier block without the two convenient holes I will do something very similar to what RockDoc has going on. I will also give the whole thing a couple coats of paint, I decided on all silver. I bought new coolant hoses and battery cables so I will get those done while the engine bay is still clear. The body lift will also go on soon.
It's amazing what I have learned in the past months. A year ago I didn't know what a crankshaft was. Here is how it sits right now,