Ok so after a bit of drama with the fuel regulator install leaking. I took it to another workshop to fix and they did an outstanding job on mounting it and piping it correctly.
I took it back to the tuner to finish the job.
He was happy with the fuel delivery after installing the pump. The line was constant/flat in his graph.
So the reading are as follows with 315s which apparently does not give the most accurate reading.
Torque 333.95
HP at the flywheel 227.1
HP at the wheel 185
So what’s the HP of the truck now ?
Boost range is from 4 to 6
Timing is set at 10
Still has a relay ticking noise down by the clutch pedal and we still haven’t figured out how to make the sub fuel tank switch work when I need it so it’s always on.
There tends to be some white smoke when releasing the gas pedal after a full throttle on the dyno. So will be adding an oil catch can to see if that solves it. If not then it’s open her up and overhaul the rings which I don’t want to do.
We kept the idle high to stop the engine from shaking from time to time.
Took it for a drive yesterday and noticed the idle is pretty high at around 2000 so will go back to adjust that and hopefully.
Overall I’m happy with the power and response and now it’s just a matter of tweaking it.