ACSD delete completed today…..
Thanks to Stiles and Hillcountry for their photos and description. Definitely a fiddly proceedure for sure. The bottom Hex bolt on the ACSD broke loose with a LOUD snap, I practically pooped myself as I thought I broke a bolt. All bolts were hosed down with PBlaster. The top hex bolt got caught up on the spring and required careful movement. I had to use a flat head screw driver to move the cold starting lever (?) forward to access the top hex bolt, the spring is quite large. I used the Back40 imports kit and everything worked great. The engine fired right up without hesitation (I primed the fuel pump with 20 plunger presses). No leaks, fuel or coolant. Also, I bought 2 new hex bolts for the ACSD delete plate. They are M6x12 and both fit perfectly. M6x16 are too long btw.
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