Put some new belts on yesterday.
Went to fire up the 3B for the first time since replacing all the gaskets and we noticed a big spark come from the front of the engine once it fired up. After some investigation we found that I had installed the idler pulley wrong, which meant that it bound up and basically welded some of the washers together as it got ripping hot. Based on the blueing of the steel, looks to have reached nearly 200-300 degrees C in a matter of seconds. We couldnāt touch it for some time as we had to let it cool.
Once we could take it off, we realized that the sleeves in the middle were not long enough to keep the outside surfaces of the bearing from rubbing the large washers. The bearing was totally fine and so were the belts. We went to Home Depot and got some M10 washers and property spaced out the pulley so that it could spin freely. Upon next start up, worked like a charm, no issues.
We were in a mad dash to finish so I didnāt take to many more pictures. The brewery had celebratory beers with our names on them.
I replaced all the old body mount hardware with some new bolts and nuts all around. I re-used the old rubber for now until I can find a better alternative that doesnāt cost $$$. The bolt supply store did not have the standard M10 x 1.25 ~100mm and ~120mm, so I got some M10 x 1.5 100mm and 120mm. They worked just fine. Put lots of lubricant in the holes to delay corrosion again.
We reinstalled the front carpets and put in the rear ones for now, as we were driving around for some sound deadening. I will be taking it all back out and laying down the butyl mat this weekend if I have time. Then I can put all the door trim and interior back together for good.
I topped up the oil with 10W-30 T4 Rotella and Prestone max life green coolant.
After some burping and checking the fluids, all seemed to work. Oil pressure was in the right operating zone, temps were steady, if not a little on the colder side. Probably need to do one more burp of the cooling system, but it needed ~12L of coolant as per the manual and it took all 12L!
As well the alternator was putting out 13.8V which is exciting that I didnāt ruin the alternator by taking it apart.
When we put the seats in, some seed (barley?) came falling out of the passenger seat. Yeah, for sure itās a farm truck.
And off we went for our first drive since October! Lots of looks and waves from people. Just a fun truck to drive and something that people love to see on the road.
It went well, the only major issue was a coolant line from the thermostat housing backed off and leaked coolant all over the engine bay. Luckily the hose didnāt blow off completely. Those 5/8ā oem hose clamps were not small/tight enough for some of the fittings. So I had to reuse some of the wire ones and some screw clamps. Not the sexiest look, but it did the trick
Back in the garage now after about 60km of bombing around town. No major leaks from any of the gasket surfaces so far! Iām pumped!!!