- Joined
- Oct 25, 2008
- Threads
- 40
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- 1,331
- Location
- Central Oregon
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- www.oregoncruisers.com
- Thread starter
- #41
Ok well I have gotten somewhere...and I have gotten nowhere.
I put the new alternator on. Fired it up and it still did not want to idle.
So I did the old carb trick where you raise the rpms up and then slam your hand down on top of the carb choking the intake out which sucks hard vac and hopefully clears out your idle circut.
Anyways after doing this a couple times my rig would not run at all hardly.
Pulled a plug and it was soaked. Tossed some new plugs in and it fired back up but was running rough.
Did the carb trick a couple more times at higher rpm and after clearing out and a couple blips its purring better than ever.
BUT! My amp meter is still acting funny! At idle with nothing running it is bouncing between neg and pos. And with a blast of throttle its pegging out still. It will eventually settle down.
Also my new regulator seems to be pumping out to much voltage.
I am going to pull it and check out the specs. I know you can adjust them but not sure what I need to tweak?
Also this is the odd ball 69 carb that was only used for a few months I believe. Is there a rebuild kit available for this carb still?
I put the new alternator on. Fired it up and it still did not want to idle.
So I did the old carb trick where you raise the rpms up and then slam your hand down on top of the carb choking the intake out which sucks hard vac and hopefully clears out your idle circut.
Anyways after doing this a couple times my rig would not run at all hardly.
Pulled a plug and it was soaked. Tossed some new plugs in and it fired back up but was running rough.
Did the carb trick a couple more times at higher rpm and after clearing out and a couple blips its purring better than ever.
BUT! My amp meter is still acting funny! At idle with nothing running it is bouncing between neg and pos. And with a blast of throttle its pegging out still. It will eventually settle down.
Also my new regulator seems to be pumping out to much voltage.
I am going to pull it and check out the specs. I know you can adjust them but not sure what I need to tweak?
Also this is the odd ball 69 carb that was only used for a few months I believe. Is there a rebuild kit available for this carb still?