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Correction from earlier, my old modulator has a black topWhat code did you see previously? With the blue, Im seeing p0402-EGR flow excessive detected. Before, it was p0401-EGR insufficient flow
What code did you see previously? With the blue, Im seeing p0402-EGR flow excessive detected. Before, it was p0401-EGR insufficient flow
I rebuilt the engine, changed every single piece of rubber/plastic on the engine, every hose in or near the engine bay, nearly every wire incl harness, modulator, cleaned the TB and intake, head rebuilt by pro shop, etc... Im thinking a piece of carbon got loose somewhere I didn't check well enough. It just seemed odd to go from insufficient to excessive. Truck idles great, no change from one modulator to another. Haven't run it through emissions since the change.I had P0401 Insufficient Flow. I changed all vacuum lines, cleaned the EGR port in the intake, and then lastly changed the EGR modulator and no more CEL. That was ~3 months ago.
I swear there was an edit button before, but damn if I can find it...
One thing (probably major thing) I forgot to mention earlier was that I hosed off the engine compartment and it ended up missing pretty mad until I got it home and checked the distributor. Rotten eggs to the max. I drove it a little once it cleared up, but no WOT for 100 miles or anything crazy.
Is the PAIR system still hooked up?
Where does the hose go, what is it hooked to?
Do you have a vacuum hose diagram?
On my '97 (your '93 may be different) the port in your second pic attaches to the EGR valve, and the end of the hose with the screw in it attaches to the EGR VSV which is the open black port on darker of the two solenoids.
Maybe this will help.
2. Leaking or bad injectors.
Well... I might have a reason for the crazy jump. Someone left the diagnostic jumper in place.
Still open to feedback though if anyone has ideas (even just aabout the diag jumper).
If the jumper was left in place the check engine light should have been flashing. If it wasn't, the light is either burnt out, been disabled or the jumper was not making proper contact. In any case there could a malfunction code like a bad O2 sensor causing a rich condition.