*Update #2*
TLC called back - Leak down test told them that cylinders #5 & #6 were at 50%
Cylinders 1,2, tested OK 3,4 tested GOOD.
He advised it was time for a rebuild.
I called back to ask about the loss of power and the rpm range not being full, he said that in fact the timing was off and the dizzy needed to be re-clocked. I told him to please do that which he said is about another 1.5 hrs labor. That should hopefully solve my issue with not running correctly.
Consumption however is a separate issue.
I asked if he would change the oil while it was there to a heavier weight that he recommended 20-50. He said "nope, your motor based off the leak down is in critical condition and if we put heavier oil in there, it may cause the rings to break."
Uhmmm - i was saying it would have been nice to know the compression on those cylinders, however he stated that i could have good compression but that wouldn't matter since the leak down didn't pass. "you might have good compression however those cylinders wont hold that air overnight, the next day it would be down at 0"
Just because i was curious, i asked and they charge approx. 20k to rebuild the motor.
I assume they will do the timing on Monday as he said "well do the timing and take the weekend and give me a call on Monday and let me know what you'd like to do"