Maybe try temporarily disconecting the wastegate to rule it out?
Follow along with the video below to see how to install our site as a web app on your home screen.
Note: This feature may not be available in some browsers.
This site may earn a commission from merchant affiliate
links, including eBay, Amazon, Skimlinks, and others.
Did you change anything with the fuel system? Have any of it apart?
I'm thinking either fuel starvation/ air in the fuel, waste gate malfunction, some form of blockage in the intake.
I think you'd hear a boost leak.
Air in the fuel will cause a stumble and white smoke out the back.
Air intake blockage will choke the engine, and also cause momentary puff of smoke out the back
Waste gate malfunction is probably less obvious.
Maybe try temporarily disconecting the wastegate to rule it out?
yesso those numbers are G-turbo?
What do you mean?What was drive pressure doing on spool up, just as the wastegate cracks?
Nice bar by the way
What do you mean?
Cheers, I got sick of being stuffed around by AOE so I redesigned it slightly and got it built on the Gold Coast
Yes, I backed the fuel off before reducing boost, it made no difference to power, just decreased spool up performanceprevious run was at how much boost PSI ..?
Did you try at 39 - 40 PSI range with less fuel .:?
I don't think it's as simple as 1 afr point, it's more to do with the drastic reduction in fuel required to decrease the boost and afr. Simply reducing the fuel resulted in similar boost with a leaner afr, and markedly increased the time taken to spool, because of the reduced drive energy. When I originally tweaked the pump, a while back, it was just a fuelling increase that changed the boost from about 33psi to 39psi, no boost adjustment was made. This time, I adjusted both, first the fuel, to reduce the black smoke and heat, and then knocked 5% duty cycle off the boost controller, which resulted in 35psi, but still with the lost bottom end and midrange performance. Had a play with the compensator, and got that back. Peak egts came right down after the fuelling reduction, and climbed much slower, even after the compensator tweaking. I do suspect the turbine was choked from the heavy fuel load, resulting in performance loss and excessive heat. Haha I'd be more inclined to blame the compressor over the intercoolerU mentioned that going from 35psi @ 19-20:1- 39psi @18:1 things got very hot very quick . 1 afr point isn't a drastic change, not enough to cause a massive temp difference . Did the boost rise to 39psi with extra fuel or did u have to adjust the waste gate . If the boost increase was with a wastegate adjustment then I would be looking to drive pressure to be the issue . The turbine might choking because the wastegate isn't opening enough plus the heavy fuel load . Drive pressure is the ratio of boost to exhaust manifold pressure. Could be compressor efficency and intercooler efficency as well .
Be somthing to monitor with your prototype too .