oregon fj
Serial rescuer of old vehicles
- Thread starter
- #21
So far today - original(?) coil mounted terminals down, during checks found some oil leaking out the HT terminal. Replaced coil with new one, mounted terminals up. No change.
While using the hand throttle to make it misbehave, manually changed the ignition timing, tried both advance and retard, no help either direction.
Pulled and looked at all 6 plugs, nothing of note. All 6 look clean and nice.
Used timing light to check consistency of spark while it does its thing. Spark appears to be consistent, no blips or skips evident.
Took a 30 second video in hopes that others might be able to actually hear it. Results are so-so. The skips and stumbles sound like pops in the video. Not sure this will be of any value.
While using the hand throttle to make it misbehave, manually changed the ignition timing, tried both advance and retard, no help either direction.
Pulled and looked at all 6 plugs, nothing of note. All 6 look clean and nice.
Used timing light to check consistency of spark while it does its thing. Spark appears to be consistent, no blips or skips evident.
Took a 30 second video in hopes that others might be able to actually hear it. Results are so-so. The skips and stumbles sound like pops in the video. Not sure this will be of any value.