OK, today was pretty overcast so I got to grips with removing the ACSD, anyone contemplating this go for it, it's a doddle!
I will not bore you with pictures as it has been done before with much better quality pictures than my old SONY can muster.
In a nutshell:
Engine cool, link the two hoses that run from the engine to the ACSD, I just run one piece from top to bottom on the block as it looks tidier and less chance of leaks.
Next I removed the idle up valve for the air con (two allen head screws) to make it easier to see what I was doing.
Next the three allen head screws holding the ACSD were taken out and about 1/2 a cup of fuel come out.
Fitted the new blanking plate with a new 'O' ring and I then
used the longer idle up screws to hold the plate on.
I then fitted the air con idle up with the
two shorter screws from the ACSD.
This will give you better thread perch on both parts.
Pumped the plunger until it went hard.....no not that plunger the one in the engine bay

.....thats it and then topped up the coolant again about 1/2 a cup.
Cranked the engine and it fired straight away, this job took about half an hour to do and that includes cleaning my tools and putting them away.
So what can I tell you so far? The ticking noise I had from the pump has GONE! That's right the fast tick tick tick that was always there when cold has left the building, so that has to be good.
The idle is still rock steady at 600 rpm unless of course the arse is pointing down hill and then it is slower
https://forum.ih8mud.com/diesel-tech-24-volts-systems/371858-odd-idle.html so no change there.
The temperature outside when doing the job was about 28 - 30 degrees so the device should not have been active anyway, tommorow I will see how it starts when it is a bit cooler, the garage is sub level but it is still about 18 - 20 so not much of a cold test but the oil will be thicker adding drag to the engine so I will be able to see how much it affects the idle.
As my fuel mileage is pretty consistent i.e. I never get less than 26 mpg

and not quite reached 28 mpg I can monitor that since the change along with the fact that my car never seems to smoke no matter how I drive it? I know the emissions test in the UK was something like 0.95 out of an allowable 3.0 so no problems there.
As I intend to get rid of the 24v starter system I need to watch for any wayward cold start moments so will be watching it pretty close so until then,
regards
Dave