- Thread starter
- #41
After looking at the two engines side by side it's pretty clear that someone did a good amount of work on the motor in the 40 and then failed to fully seat the dizzy and melted the motor. The dizzy in the 40 sticks up a full inch higher than the running F. As for the compression on the new motor, it was free and I want to drive not wrench, so it's going in so I can take the kids to the beach.

