The biggest problem they ran into was finding cam-bearings. Evidently the part they kept ordering had the wrong OD, but they eventually got the right one from specter. They also had trouble sourcing valve guides, and eventually wound up getting a too-large set of them and machining them down. I drove the truck home yesterday, and it felt great, but by the time I got it home it was leaking oil and idling a little ragged, so it'll probably go back to them today or tomorrow. The work _looks_ super clean, and it sure ran nice on the way home.
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