Try the timing. Its easy. There are many variables in timing-even slightly mis-machined keyways for the crank and balancer/ mis stamped timing marks/ machining of cam/ gear at cam attachment/Timing chain stretch/advance curve/etc/etc.
Follow along with the video below to see how to install our site as a web app on your home screen.
Note: This feature may not be available in some browsers.
This site may earn a commission from merchant affiliate
links, including eBay, Amazon, Skimlinks, and others.
Ok I haven't read the entire thread
Have you:
1: Replaced front O2 sensor
2: Checked logged AFR when it happens
3: Was the head and block decked? If so how much?
4: Find/Rent a borescope and pull the spark plugs and check the top of the pistons for build up or any damage.
We will agree to disagree - The timing might not be the entire causative factor, but could contribute to it.
Also because their are different levels / amounts of detonation at different load points when you are driving and you can't determine how much you are getting.One thing I will promise you is that you are getting more detonation running more advance. I you have detonation at 3 or you will have more at 6 degrees as you shorten the knock threshold.
You also start diagnosing and making changes from stock configurations. Trying to find your cause running an extra 3.5* of advance is throwing money, time and effort away.
Just trying to help.
agree with this, you should be diagnosing at the fsm set levels on everything, otherwise you are imparting other variables into the equation.
That I do not know. No way of telling without removing valve cover, correct?A thought: Any chance the valve clearance may be a little tight? Exhaust valves more so than intake transfer heat back to the head when they're closed, and a tight valve or two will run a tad warm when at operating temp, sometimes even causing detonation.
1) YesAny answers to these easy questions?
1) Yes
2) I have no way, or even know of a way, to do that
3) heads never been off so no
4) have not done that
2) and 4):
If the AFR is off, or if there was damage to piston, changing octane would not have an effect, correct?
Just so it's clear, timing is set to factory 3*. It has been at 3* since last summer. When it was at 6-7* the rattle was no better and no worse.
Thanks.
1) Yes
2) I have no way, or even know of a way, to do that
3) heads never been off so no
4) have not done that
2) and 4):
If the AFR is off, or if there was damage to piston, changing octane would not have an effect, correct?
Just so it's clear, timing is set to factory 3*. It has been at 3* since last summer. When it was at 6-7* the rattle was no better and no worse.
Thanks.
That I do not know. No way of telling without removing valve cover, correct?
Would it pass state inspection of it's running lean? I just got it inspected last month And it passed. How would it be running lean enough to have this problem but have no other problems and no CEL?No that is not correct. Octane rating is directly related to antiknock properties. If you're on the edge because of lean condition, build up on the piston/combustion chamber (raising compression) or a sharp edge because of piston damage higher octane will help prevent it.
You say you have done everything but these are certainly things I would want to check right away if I had the issues.
Get an AFR gauge and have a bung welded in before the Cat or get one that clips into the end of the tailpipe just know that it will probably read a little leaner than true because of the cat.
Exhaust is pressurised . Be hard to leak air in. Just back off the timing a couple degrees.
Like reelitchy said, I've monitored it on my Scangauge and the voltage values are always where they should be. But, I think you said somewhere that it needs to be checked in wideband??? I could be wrong about that, though. I understand wideband is more detailed but if wideband detail is what the ECM needed then wouldn't it have wideband O2's (I don't think they were even available in 1997, though). I just can't wrap my head around, and neither can the 2 mechanic-ish friends I talked to about this today, that it can be running lean with no CEL and the O2 values reading properly on the Scangauge.Running lean would make it pass state inspection with flying colors. The narrow band O2 should catch a lean condition but they are very marginal. I have seen many people have problems with their O2 sensor and no CEL's.
, I always get that backwards.Even if it did add air ahead of the O2s it would give a false lean reading (too much oxygen/not enough burned fuel) -then richen the fuel mix-creating an artificially RICH fuel/air in the chamber. That would cool the chamber temps and resist pinging.
IF it was valves then ambient temp would change if it rattled or not? The guy who owns the head shop (bad name. It's actually a mechanic/machine shop that specializes in head work) said ambient temps would have no effect on it if it rattled or not. Said one problem at idle and cool or another problem when warm. The ambient temp wouldn't be a factor, much less THE factor, in wether it did it or not. Hope that makes sense. You're saying ambient temp can 100% effect it happening or not if its valves? Thanks."I just spoke with a guy that owns a head shop in the town I work. He says its not valves so that's 100% out."
I'm sorry, aside from the initial reaction I had about the guy who owns a head shop (Gas Pipe?) I don't understand why you can throw out something because a guy told you so when you haven't verified the correct valve clearance. After all you've been through in chasing this issue down, it seems to me that it might be something you would want to either rule out through hard evidence (correct valve clearance at operating temperature) or possibly find a cause for the problem. Heck, a valve clearance check and adjustment if necessary is part of a 60k service. Tight valves (insufficient clearance) will cause detonation, and if severe enough, burned valves, especially on the exhaust side, because they're not in contact with the seats long enough to properly cool, and a localized hot spot in a combustion chamber will cause detonation.
I realize your contact owns a head shop, but I'm trying to offer suggestions based on close to 30 years of being a professional service tech with certifications from two manufacturers and at least one independent professional organization to the tune of Acura Master Tech & NSX Tech, Lexus Master Tech, and ASE Master Tech (L1). Granted I've been out of the field for a while and didn't do much in the way of run problems while I had my shop since it was mostly gear work and fabrication, but some things about the internal combustion process and the machinery involved are universal.
Obviously it's your truck and your problem, and yours to troubleshoot as you please, but with absolutely no hard feelings and with all due respect, I must bow out. I sincerely wish you the best of luck in finding your problem.