To be able to get more boost I needed more fuel and the diaphragm lift pump wasn't going to cut it. I read somewhere that suggested the diaphragm style lift pump (if it's healthy) was OK at supplying fuel to the VE to reach mid to upper 30s in boost. Since my target boost with the twins is higher it was time to upgrade.
This is the old.
Here is the new. I found this on ebay for a pretty good price. It is a genuine cummins part and it came with two gaskets. It was in a sealed bag and the pump had been lubricated before it was put in the bag. You can kind of see the two plugs that are in the inlet and outlet. They were label with the hole size which I thought was a nice touch. The inlet is 1/2" npt and the outlet is 14x1.5mm
Close up of the part number 4988747. This is for a 2nd gen 5.9 cummins and is a high pressure pump.
The same day my replacement spring from thehungrydiesel.com showed up and it was very simple to swap out. The new spring did not have the rate of the old spring. You can see that the original (the black spring) has thicker wire gauge than the replacement (the silver spring). Again I chose a 15psi spring considering the boost I wanted to push with the big injectors I'm running.
Using one of the included gaskets as a template I cut out a spacer from 3/16" plate I have.
Here's the new pump with a 3/8" hose barb converted from 1/2" npt on the inlet. I reused my old pump's bolts and have the spacer plate I made with gaskets mocked up in this pic. I test fit the pump without the gaskets at first to see how it fit. As suspected my crankcase breather catch-can needed to be moved for this pump to fit so I took it off for the time being until I adjust the mounting bracket down. With the pump in place I was able to see how the hardline from the pump outlet to the main filter would fit.
I upsized the fuel line from my pre-filter to this pump to 3/8". My pre-filter pump head was also 1/2" npt so I picked up two of those hose barbs to make it work. I was looking for SAE J30 R9 hose but I was able to find some compatible fuel line at a local auto parts place. In case I run biodiesel I wanted the hoses rated for it and all my other fuel lines are rated for bio.
My original hardline from the lift pump to the main filter physically fit but needed to be reshaped. I played with bending it but in the end I cut it and used the ends for the fittings. I replaced the center section with 5/16" fuel line and that gave me the flexibility I wanted. At some point I may redo this section with some ~AN fittings but for now this works fine. It will be an easy place to put a fuel pressure gauge as well. Since I'll see a max of 15psi on this line simple hose clamps have been happily keeping it sealed.
I also opened up the holes on the banjo bolt to 11/64 for a little more flow potential.
Piston pump installed. A little hard to see the hardline that I turned into a soft line but it's there.
Results:
I have not hooked up a fuel pressure gauge yet but just by installing the new lift pump I gained about 40-50 rpm on idle. Without changing any fuel settings I took it around the block but it was still low on power and boost. The last thing I did not try was to bypass my MBC. Once I got that bypassed I was back in business and I noticed it was stronger on the upper rpm range as well. I replaced the new stiffer spring I had put in the MBC with the softer one I started with and boost could be built again and power was up. So while the MBC was causing a fueling issue because its spring was too stiff and requiring too much boost to overcome its setting thus causing the AFC to not add more fuel as boost rose, the new piston pump with more pressure and volume is going to better support the boost that I'm after and keep the VE supplied to keep it healthy.
With my fueling cleared up I continued with more tuning. I added a full turn in on the full power screw and took it for a spin. Now I was hitting some kind of wall with the total boost gauge. It would increase up to 30psi and then stop. The gauge would also hang when I let off the throttle and then decrease abruptly. I dug back into it by removing the signal line at both ends and blowing it out with high pressure air from the shop compressor. I then regulated the supply to 60psi to test the gauge holding a rubber tipped nozzle to the gauge inlet to create a seal. I go the gauge to operate correctly and decided to hook it all back up. There must have been something in the line because it's now working fine.
For my latest tuning adjustments I left the full power screw as it was, 1/4 up on the starwheel, 1/4 up on the smoke screw, bumped timing to 18 degrees, and played with a couple different springs on my springgate. I was surprised at how stiff the spring needs to be to get the PR ratios I'm looking for. I got some more springs to play with and ditched the dual rate idea. So far I'm at a .080 WG 1.75" long spring
So with my latest tune here are my results: I'm seeing a total boost of 45psi with 21psi coming from the primary.
Total psi 45 = total PR 4.06
Primary psi 21 = primary PR 2.43
Secondary PR 1.67 = Sec psi 9.9
~10 psi total at cruising (~65mph) with EGTs at 750F. On my WOT assaults to see 45psi I barely touched 1000F. I think this will climb a little more on highway grades. Making the secondary do a little more work has brought the EGTs down some along with the timing bump. And it's cleaning up to a reasonable haze. I'm much closer than I was two weeks ago but I've got a little bit more to go. I might drive it for a week or two at this tune to see how it sits.