J, someday I'll get that side shot pic on level ground. I haven't forgotten about it.
Time for some updates:
I've been doing some camping with the family. Here we're at the coast helping out a youth group.
Dora did some trailer duty and just hung out throughout the summer. The wife and I met up for a family thing in different vehicles one time and on the way home I had her drive the truck so I could check it out. I noticed it was hazy pretty much most of the time and I don't have the pump turn up excessively. Short story is failing injectors and some tired valve springs. I stepped up to 60 lbs springs for both intake and exhaust. While the package was in transit I prepped things by removing covers, removing rocker arms, and pulling out the injectors. Then I covered it up until the package arrived the next day.
There are different ways to keep the valves shut while pulling the springs off. I decided to use air pressure so I opted for the HF compression kit to use it for the adapter and parts. I cut the line and put on a quick disconnect for air. Tested it for leaks and had no issues.
The bottom right adapter in the kit is the correct thread but the lower part doesn't fit into the injector hole. I clearanced it and if fit just fine after that.
I measured the body of one of the stock injectors I pulled out to know how much material to remove.
So my plan was to use this adapter to supply air into the cylinder through the injector hole to keep the valves shut and not fall into the engine. I struggled with it and after some head scratching I figured out that this was for compression testing and that there is a little valve in the connection fitting that I needed to remove. Duh... Once I figure that out it worked fine.
The springs showed up so I borrowed a valve compressor and started the swap. I took my time, kept a little magnet pencil close by to grab the collets once the retainer slipped down far enough to expose them. I kept holes in the head covered to reduce the chance of losing one of those little guys down into the depths of the cummins.
Here's a new spring being compressed to fit it on the valve and slip in the collets. I opted for no gloves since I didn't want one of those collets slipping out of my fingers and not knowing it.
Spring gone and 150 psi of air holding up the valve.
Old spring on the left, new installed spring on the right.
Uninstalled spring comparison. New 60 lbs spring on the left, old stock spring on the right.
Success, all the springs have been swapped with only one or two stray words leaving my mouth.
This is how I supplied my 150 psi of air. Not quite sure how much I started with but I estimate I used maybe a 1/3rd of it. The rest in my 15 lbs tank will probably last the rest of this season.
Reinstalled the rockers, torqued down the studs, set up the valve lash and put on the covers.
Next I'll get into injectors.