Understanding that in these repairs I stand on the shoulders of giants (
@TeCKis300 and others)...
I suspect that my
biggest issues were the actuator's poor/inconsistent contact at the microswitch
View attachment 3046437(might be submicroswitch), and possibly the corrosion at the concentric electrical contacts. Disclaimer: I'm not a mechanic or doctor, and the Holiday Inn Express here is occupied by violent squatters; don't do this stuff unless you are ready to buy a new transfer case actuator assembly. For inspiration and to steel my nerves, I watched
KenKej savagely restores these parts.
- concentric electrical contacts
- motor
- tested fine on 12v bench test; saw no need to remove/break factory solder points
- removed the big silver screw (south-end in picture) to remove the bracket
- removing the bracket uncovered the small hole in the motor
- covered and isolated motor with shop towel in same way as the switch (see pic below) and sprayed CRC Lectra-Motive Elecric Parts Cleaner inside, holding the motor-in-housing hole-side-down.
- microswitch
- required several removal/install cycles for me to figure out and to fixView attachment 3046441
- escalated to switch dissasembly; plenty of corrosion found in spite of having a relatively clean actuator housing
- turns out the issue was twofold: corrosion at contacts and too-loose hinge mechanism
- the tiny plastic hinge allowed z-axis travel (orthogonal to intended plane of travel) of the platstic arm, making good contact at full-up or full-down positions but wildly inconsistent Ohm readings at its resting plane/position.
- did not have the talent/bravery to mess with plastic housing of microswitch to reduce the up-down looseness
- did have sufficient recklessness to gently adjust the two copper arms 'upwards' (on workbench), downwards when in-situ, to improve firmess of copper-on-copper contact when switch is activated by rotation of actuator wheel.
- how gently did I manipulate those copper arms? If you are reading this and are thinking about doing this, you are already using too much force.
View attachment 3046442
Over the course of this repair attempt I un- and reinstalled the two actuator housings many times. I want to share some things that would have helped along the way, had I known them earlier. Credit to sixweeds over at tundras.com for great work on this issue with the Tundra cousin truck (
among other info).
Next time I will remove the entire actuator housing (yes,
can be done without dropping/cracking, etc.) to
- more easily service both CDL and 4LO actuator housings
- allow spray of penetrating oil into the push-rod housing/channel. I think they become less compliant over time, which causes the electronics in the actuator housing to work harder and degrade faster
The poaster over on tundras linked to a few good videos from a Tagalog-speaking mechanic in Saudi Arabia. The videos are all shot with the front-facing camera, so I grabbed the stream, inverted, and will drop the reinstallation gear-clocking information here. (
original video)
Bottom line on installation: push the actuator rods
all the way in. (NB: my truck was in 4HI w/ CDL not locked)
Clock gears as follows. And use a screw driver (or other long, flat thing) to hold gears in place while installing top-side housing. You
may have to adjust the clocking slighly to line up with shaft teeth. Do so by pulling the housing, turning the larger gear below the motor, and going in for second approach.
View attachment 3046450
Hope I'm not posting Captain Obvious(tm) stuff here, but it's likely. These are the things I wish I had known before doing the work, and hopefully they will, in turn, help someone else. Again, hat-tip and thank you to
@TeCKis300 and
@cogniz et. al here, that Tundra wranger sixweeds, and my boy KenKej on the tube.