Steering Rack Rebuild (1 Viewer)

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ndg

Joined
Feb 26, 2024
Threads
1
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26
Location
UK
First off, this isn't a comprehensive DIY - the process is outlined in the workshop manual, but I thought I'd run through the things I found along the way as I haven't seen it covered elsewhere. My truck has always been a bit 'juicy' in the rack gaiters, but started leaking PAS fluid from the pinion input seal in a more significant way a month ago. Not horrendous, but these things only get worse and we're off on a trip to the Alps on Friday. It was also likely to cause it to fail it's MOT (UK annual safety check) tomorrow so needed sorting.

Removing the rack has been covered in a few places (forum.ih8mud.com/threads/how-to-replace-your-own-steering-rack.560104), but as I was planning to rebuild and my inner tie rods/gaiters were good I removed the inner ball joints from the rack shaft to make it shorter, steered the rack full RH. I then lifted the engine off the LH engine mount and my RHD rack came out without touching the oil filter or its housing.

Removing the transfer pipes went okay - I used knipex parallel jaw pliers as they let you really clamp down on the flare nut to prevent slipping.

Next step was to unbolt and remove the pinion housing. That's all the instructions provided by Toyota. I'm sure that's how it works on a nearly new rack or one that lives in CA. However even though my truck is pretty good from a rust PoV the pinion housing was jammed solid. I finally got it out by quickly warming the rack housing up to 100C then rotating the housing fore and aft with plus gas sprayed intermittently into any crack. As the heat in equalised between rack and pinion housing it would become tight again and I'd have to wait for everything to cool and start again. I had to do three heat cycles to get it moving freely enough for the next step. This was the same but with the housing rotated 90deg so I could get the wife to apply a prybar under the flange whilst I wiggled, alternating from side to side to walk the housing up and out. Again this took three heat cycles as everything tightened up as the differential expansion effect wore off.

Hanging on to the pinion housing to rotate it was a challenge as there are no flats and plenty of features that you don't want to damage. I made a giant pin spanner from scraps around the garage. The pins are 8.5mm diameter (turned down from a 10mm bolt), welded into a 12mm chunk of steel that was hacked about to give clearance around the housing. I then welded a ~1m bar to it for leverage. It's not pretty, but it did work. It also made for a good work holding fixture for the next step.
PXL_20250607_184423048.jpg
PXL_20250607_184444001.jpg


The pinion housing nut needs a special tool. It has to be hollow to clear the pinion, with a 32.5mm 8 sided 3mm deep 'nut' feature to engage with the internal form. I put a 32mm hex on the other end to grab with a socket. This worked a treat.
PXL_20250607_195823792.jpg
PXL_20250608_090152368.jpg
PXL_20250608_095620709.jpg


All of the Teflon rings looked good in my rack (and I didn't have a sizing tool for the new ones) so I left those as is and just resealed with OEM Toyota seals. The only exception to this was the pinion input seal which was on backorder. As I was up against time I ordered a Corteco replacement part - this had the same manufacturer and part number as the OE seal that came out so happy that it's a quality part, even if the manufacturer is NOK!

You'll also need a selection of specifically sized drifts to knock the oil seals out of and in to the pinion housing and rack body. The manual states to press the seals in and out. I did this for the pinion housing, but my press isn't tall enough for the rack housing. Tapping them out and back in with a hammer (carefully) worked fine. I made sure that all tools that went into the cylinder were smooth and burr free to avoid scratches, aluminium where possible and a coating of ATF doesn't hurt either. There's a special tool called out in the instructions for pushing the seals over the rack ends. I just taped up the ends of the rack with electrical tape - there's a taper onto the main part of the shaft, so the tape just protects the seal from the sharp bits at each end and doesn't increase the effect OD and risk stretching the seal.

Reassembly was straightforward and once the corrosion was cleaned out of the pinion housing it slotted straight back in easily (this time with a little grease).

All back on the truck now and no leaks so far. 🤞
 
Excellent work! I have rebuilt a steering rack on a Porsche before, but the pinion seal/nut was on the shaft side unlike the Toyota. Would you be willing to sell the pinion seal socket, or possibly make them for the community? I am sure if you are not interested there may be a vendor on here that would pay for your intellectual property.
 
First off, this isn't a comprehensive DIY - the process is outlined in the workshop manual, but I thought I'd run through the things I found along the way as I haven't seen it covered elsewhere. My truck has always been a bit 'juicy' in the rack gaiters, but started leaking PAS fluid from the pinion input seal in a more significant way a month ago. Not horrendous, but these things only get worse and we're off on a trip to the Alps on Friday. It was also likely to cause it to fail it's MOT (UK annual safety check) tomorrow so needed sorting.

Removing the rack has been covered in a few places (forum.ih8mud.com/threads/how-to-replace-your-own-steering-rack.560104), but as I was planning to rebuild and my inner tie rods/gaiters were good I removed the inner ball joints from the rack shaft to make it shorter, steered the rack full RH. I then lifted the engine off the LH engine mount and my RHD rack came out without touching the oil filter or its housing.

Removing the transfer pipes went okay - I used knipex parallel jaw pliers as they let you really clamp down on the flare nut to prevent slipping.

Next step was to unbolt and remove the pinion housing. That's all the instructions provided by Toyota. I'm sure that's how it works on a nearly new rack or one that lives in CA. However even though my truck is pretty good from a rust PoV the pinion housing was jammed solid. I finally got it out by quickly warming the rack housing up to 100C then rotating the housing fore and aft with plus gas sprayed intermittently into any crack. As the heat in equalised between rack and pinion housing it would become tight again and I'd have to wait for everything to cool and start again. I had to do three heat cycles to get it moving freely enough for the next step. This was the same but with the housing rotated 90deg so I could get the wife to apply a prybar under the flange whilst I wiggled, alternating from side to side to walk the housing up and out. Again this took three heat cycles as everything tightened up as the differential expansion effect wore off.

Hanging on to the pinion housing to rotate it was a challenge as there are no flats and plenty of features that you don't want to damage. I made a giant pin spanner from scraps around the garage. The pins are 8.5mm diameter (turned down from a 10mm bolt), welded into a 12mm chunk of steel that was hacked about to give clearance around the housing. I then welded a ~1m bar to it for leverage. It's not pretty, but it did work. It also made for a good work holding fixture for the next step.
View attachment 3925126View attachment 3925127

The pinion housing nut needs a special tool. It has to be hollow to clear the pinion, with a 32.5mm 8 sided 3mm deep 'nut' feature to engage with the internal form. I put a 32mm hex on the other end to grab with a socket. This worked a treat.
View attachment 3925128View attachment 3925129View attachment 3925130

All of the Teflon rings looked good in my rack (and I didn't have a sizing tool for the new ones) so I left those as is and just resealed with OEM Toyota seals. The only exception to this was the pinion input seal which was on backorder. As I was up against time I ordered a Corteco replacement part - this had the same manufacturer and part number as the OE seal that came out so happy that it's a quality part, even if the manufacturer is NOK!

You'll also need a selection of specifically sized drifts to knock the oil seals out of and in to the pinion housing and rack body. The manual states to press the seals in and out. I did this for the pinion housing, but my press isn't tall enough for the rack housing. Tapping them out and back in with a hammer (carefully) worked fine. I made sure that all tools that went into the cylinder were smooth and burr free to avoid scratches, aluminium where possible and a coating of ATF doesn't hurt either. There's a special tool called out in the instructions for pushing the seals over the rack ends. I just taped up the ends of the rack with electrical tape - there's a taper onto the main part of the shaft, so the tape just protects the seal from the sharp bits at each end and doesn't increase the effect OD and risk stretching the seal.

Reassembly was straightforward and once the corrosion was cleaned out of the pinion housing it slotted straight back in easily (this time with a little grease).

All back on the truck now and no leaks so far. 🤞
Great write up! I did this job when I had my engine out - I 3D printed a tool to get that octagon pinion housing nut off & it worked really well. My truck was 100% rust free though, so that likely helped! Did you have to put much force on yours?
 
The octagon nut wasn't too bad as it's protected from the elements. It was just the pinion housing that was a nightmare.

I hadn't thought about a 3D printed option. But can see it working for irregular use. Sounds like there could be interest if you add it to your shop.
 
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Unfortunately this seems to be NLA from Toyota.

The 'variable open wrench' (09922-10010)
comes up quite a bit in the jobs I've done so far. It's £106 from Amayama, probably £150 by the time it's delivered though.

What's 0961600011 used for? I can't see it through the bag!
 
Unfortunately this seems to be NLA from Toyota.
Which one?
The 'variable open wrench' (09922-10010)
comes up quite a bit in the jobs I've done so far. It's £106 from Amayama, probably £150 by the time it's delivered though.
It does. I like that it has 10mm nut on span drive, to really bear down. Also it has also two 3/8" drive socket, useful for torque wrench. But, I use the forged wrenches more than it. Which they're better at breaker taught threads lose.
What's 0961600011 used for? I can't see it through the bag!
Setting pinion preload. Fits over input shaft.
IMG_6135.JPEG
 

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Which one?

It does. I like that it has 10mm nut on span drive, to really bear down. Also it has also two 3/8" drive socket, useful for torque wrench. But, I use the forged wrenches more than it. Which they're better at breaker taught threads lose.

Setting pinion preload. Fits over input shaft.
09631-20060 is seemingly NLA - the octagon drive.

I did wonder if the one in the packet was the preload socket. I reset preload to the original location and then checked and adjusted in the car by feel. I made a shallow 56mm socket for that job a few years ago, not sure it works on LHD though.

Because we were talking about it I had a look for the variable open wrench yesterday and found a used one on ebay for £47, looked in decent shape in the photos, so got that bought. I had bought a cheap aluminium version a while ago, but it was rubbish, keft deforming at low torque and I finally exploded the jaw trying to loosen the pinion housing!
 

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