So with an August long weekend camping trip around the corner, the push was on to finish this thing. The clutch line solution for the time being was a combination of re-bent RHD lengths and a PRICEY length of braided stainless hose I had made up. We bled it and got the clutch working, plugged in the transfer case connectors, installed the driveshafts and flashed it up. Idea being make sure it works, then tackle the "little" things like shifter bending and trans tunnel cover etc.
10pm the night before. Check fluids, start it up. It's on the hoist. I put it in first, let the clutch out, then 2nd, then 3rd, then 4th, then 5th. Great. Reverse. Reverse?
No reverse. No grinding, no stiffness, no noise, no drive to the wheels. Shifter is falling all the way into place. No reverse to be had.
Dejected, we packed up for the night and my friend and I took her Jeep JK of Shame camping that weekend instead.
SO, the following week, after reading
this H151F rebuild thread I saw that the reverse gear was in the rear housing, aft of the intermediate plate which provides the backbone for the transmission. So I undid the driveshafts, supported the trans with the jack, took the transfer case off, undid the crossmember and pulled the rear housing off (after draining the fluid). My thoughts being, if reverse isn't engaging I should be able to see why right away if I popped this cover off.
Lo and behold:
View attachment 2828089
View attachment 2828090
View attachment 2828091
The reverse gear selector fork was shattered. That explains it.
I was feeling pretty rotted and sent the guy who shipped it to me an email asking if he'd known about this, of course he said he didn't and it's very possible that was true. In any case, I'd need to find a new fork or have this one repaired. I took it and its pieces to one machine shop that told me where I could go, another machine shop said they'd do their best with it. In the meantime I looked and looked until I found a listing on Megazip new OEM for $75 so I ordered it. When it showed up it looked different than the original, and the machine shop (Velocity in Burnside) had done a beautiful job on the original, so I opted to put the original back in.
After rushing to put it all back together before I left for work the following day, I realized I'd forgotten a circlip on the output shaft and would need to take it all apart once again to reinstall it. Oh well, I'd tackle that next month.