- Joined
- Sep 28, 2002
- Threads
- 559
- Messages
- 8,120
- Location
- Kamloops, BC Canada
- Website
- www.shopraddcruisers.ca
Well its a bit of chit and chat along with very little tech.
David from Santa Cruz called my last week and was visiting up in Whistler, once his visit was completed he shot down the sea to sky highway and jumped on a ferry to Nanaimo.
Once here we went through some glow issues and quickly solved that problem(which never happens when it comes to electrical).
Moving on we rebuild it leaking clutch master, for some reason we had a hard time getting it to flow, dissassembled it a second time and re assembled to our surprise it flowed???
Dropped some new brushes in the alternator and it seem to fix the low voltage problem.
Once that was fixed we noticed a very leaky coolant hose, the coolant was a brownish sandy colour, after flushing and replacing the line and refilling his engine with new coolant he was good as new.
David told me his fuel return rail was cracked and he had JB Welded the sucker, I was pretty sure the tinny return line would be plugged, it was his lucky day as I had a spare kicking around so I gave it to him.
The high roof righ hand drive vehicle was the first I ever drove and found it surprisingly easy to master, short of the turns signal and windshield washer.
Nice rig...............
David from Santa Cruz called my last week and was visiting up in Whistler, once his visit was completed he shot down the sea to sky highway and jumped on a ferry to Nanaimo.
Once here we went through some glow issues and quickly solved that problem(which never happens when it comes to electrical).
Moving on we rebuild it leaking clutch master, for some reason we had a hard time getting it to flow, dissassembled it a second time and re assembled to our surprise it flowed???
Dropped some new brushes in the alternator and it seem to fix the low voltage problem.
Once that was fixed we noticed a very leaky coolant hose, the coolant was a brownish sandy colour, after flushing and replacing the line and refilling his engine with new coolant he was good as new.
David told me his fuel return rail was cracked and he had JB Welded the sucker, I was pretty sure the tinny return line would be plugged, it was his lucky day as I had a spare kicking around so I gave it to him.
The high roof righ hand drive vehicle was the first I ever drove and found it surprisingly easy to master, short of the turns signal and windshield washer.
Nice rig...............