After the exhaust was done, I buttoned up some things in the engine compartment, tuned the propane and adjusted the timing over the weekend.
Ducked out of work early Monday (leaving Tuesday morning for CMCC '14) for some last minute parts pick-up and final prep for vacation. The front driveshaft, which was a lengthened factory Toyota mini DC shaft, had to be run backwards because apparently Toyota used different pattern flanges for the diff and t-case ends. Not a big deal. Dumped a bunch of tools in a bag, searched for recovery gear, gave a final walk around and loaded onto the trailer.
Coal Mine '14 trip report...
Day 1, Wednesday. I ended up leading a group for green/blue trails, which gave me a perfect opportunity to lightly break things in and check for obvious bugs. The first thing I need to fix is the front shackles are using the frame as a bump stop. At rest, they have a nice angle to them but evidently the springs have more up-travel than I thought.
Day 2, Thursday. Blues are boring, lets do blacks! For the most part everything was point and shoot. 75% of the day was spent in 2wd rear. Spools are awesome. With the front tires stuck in a watery pit and the rear trying to climb, I blew the lower radiator hose off the block. Clamped it back on, refilled with some North Carolina water and winched out. About 50’ further, the steering shaft decided it didn’t want to be attached to the steering box anymore. Another simple, yet cramped fix. Finished that trail without another incident. Onto the next trail… about a half hour into the trail while climbing, the front suspension dropped out and left the driveshaft splines engaged by fractions of an inch. The suspension recompressed, driveshaft tried to do the same but instead egged out the female end of the slip and shock loaded upstream through the transfer case, found the weakest link and cracked the t-case adapter 180* around the bottom. I attempted to back down but the transmission and adapter were trying to separate themselves. Winched backwards and towed out the only rig strong/heavy enough...GLTHFJ60's unlocked 4BT FJ60 on 1 tons. Was a painfully bumpy ride for sure. The carnage obviously sucked, but knowing that I no longer have to rely on my wheeler to get me to work anymore made everything just a little bit more tolerable.
About 50 yards from the parking lot… PRANG! I see a tow strap and a kinetic strap flying through the air and something big and metal smash into the windshield frame directly in front of my wife's face. She was a little shaken up. My first thought was one of the recovery points I welded to the front crossmember/bumper failed. Hopped out and see the tabs are still there and show no damage, straps didn’t fail either. Come to find out the threads stripped out of one of the d-rings on my end. Yes they were checked prior to hooking everything up, and no they weren't some Chinese off-brand POS... but a very well known winch company who probably still has shackles made in China. Winched myself onto the trailer and there it sat for the rest of the event.
Day 3, Friday. Got to spend the day spotting which was fun. Unfortunately near the end of the last trail, the aforementioned tow truck snapped the rear output yoke on his Dana 300 which resulted in a combination of 1 wheel drive, winching and towing to get to flat ground.
Some pictures…
Radiator hose go boom
Me and the eventual tow truck
Broken!
All in all, I couldn't have been happier with how the truck worked (when it was still operational). Tires hooked up real well, first gear/low range is great, my wife didn't feel the need to get out when I tried something stupid, and I was finally back in my own truck.