High flow power steering pump (1 Viewer)

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Apparently the fluid foams and there is not sufficient distance for the bubbles to break before returning to the system. The PSC reservoir has an internal filter which is supposed to stop the foaming before returning back to the system. It is only theory on my end until it is installed and running. Crossing my fingers that it will resolve this issue.

For the steering, and I am not sure but would think you are pushing more fluid which would exacerbate the issue.
I would disagree. Toyota designed this reservoir to not aerate the fluid by design. With my new reservoir I see fluid moving, but now it isn’t spilling out with the lid off. I took apart my old reservoir and see the screen/internal filter was discolored and seemingly partially blocked. I would venture a guess most 80 owners have this issue, but it isn’t as compromising as mine. Coming from the dealership world I don’t know of many brands that even call for a power steering fluid flush maintenance interval from the factory. Most older Toyotas that I’ve worked on over the years have really dark fluid in the system and it’s probably never been touched. Normally these systems are insanely reliable, but given the age and the fluid breaking down overtime it tends to wear the veins in the pump as well as cause the rubber components to break down. I recommend everyone replace that fluid every 5 years or so. And to whoever mentioned it, properly bleeding your new components in the steering before starting the truck as you will cause premature damage. I reverse bleed my systems with a vaccula connected to the return hose so new fluid is sucked in as the old is removed.
 
There products tend to be thick. Clean that strainer and go with proper ATF.

Pulled the reservoir apart. Great call man. Here is what I saw…

- Lots of old sludge in the bottom of the reservoir
- “Outer” screens had blockage for sure
- “inner” screen and the “horn” had lots and most of the blockage (see pic after 2 cleanings… it’s spotless now)
- that Lucas is way thicker than regular atf (going with mobile 1 …. Tell me if I am wrong… I’m oil dumb)

Plan is to use the low pressure return to cycle out all the Lucas crap for the new stuff

Cheers 🍻 and thanks

Edit: added the pic

IMG_6847.jpeg
 
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Pulled the reservoir apart. Great call man. Here is what I saw…

- Lots of old sludge in the bottom of the reservoir
- “Outer” screens had blockage for sure
- “inner” screen and the “horn” had lots and most of the blockage (see pic after 2 cleanings… it’s spotless now)
- that Lucas is way thicker than regular atf (going with mobile 1 …. Tell me if I am wrong… I’m oil dumb)

Plan is to use the low pressure return to cycle out all the Lucas crap for the new stuff

Cheers 🍻 and thanks
I’ve been into 80’s for 11 years and all I have used is Dex/Merc.
 
Reporting back….
- Reassembled the reservoir
- I did the lazy man’s fluid swap through the low pressure line - worked great - swapped out 2 quarts
- Bled everything with ignition in ACC position
- Started truck and did the same bleeding procedure (with the cap off and the fluid was NOT shooting out of the reservoir like it was before I cleaned it)
- Testing - everything was way smoother, faster and that “stutter”/lockup I had when turning left is GONE!
- Overall, the power steering seems waaaay happier and has zero noise or groan

If just the cleaning of this reservoir and inner baffle/screen/filter fixed the issue @baldilocks …. I might you a lot of beers (I was about to start throwing money at this issue!).

One comment…
All the crap caught in the screens… my truck has 350k on it. The high pressure hoses were breaking down super bad. My guess is that this crap in there is from the interior of those hoses (total guess but may make sense).

This forum is awesome. 👏🏻🍺🍺🍺
 
Glad you got that squared away. I would agree that much of that debri was from deteriorated hose.
 
Glad you got that squared away. I would agree that much of that debri was from deteriorated hose.
Are you headed to Rubithon? I will pack extra beers for gifts 😁🍺🫡
 
I wish I could go to Rubithon. Haven’t been since 2018 but I normally go there once a year anyway. I used to live in Vacaville for 30 years and been going to Rubicon since 1990. My previous 80 was flopped at 25 mph in 2023 so I scrapped it, bought another one that year and am still in that total rebuild process.

I just happy you seem to have fixed your issue without needing to spend a bunch of greenbacks.
 

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