As I wrote in the first post, the radiator has been fully rebuilt. The thermostat has been replaced, the water pump works and I have a new one as well, and before I changed the mechanical fan, the fan clutch had good viscous fluid in it. At this point, there isn’t anything left but the cracked head leaking exhaust gas into the coolant that could be the problem. The engine was overheating with all the stock coolant components before I started changing things (ie, different air filter, electric rad fan, intercooler). Correct me if I’m wrong.