Hello!
My upper radiator hose popped off and dumped coolant. Engine temp needle went to about 1/4” from the lower edge of red on the gauge for about 30-60sec before I cut the engine off.
Engine has run fine since - for about 10 days since losing coolant - but developed a coolant leak (no evidence of oil & coolant mixing) with the strongest flow while cooling down. It would leave a small puddle about 6” across over the course of 20-30minutes after turning the engine off.
I tracked the leak to the second to last lower intake manifold bolt so I pulled the manifold today expecting to see a crack in the head but it’s not showing anything that would produce a leak, at least not on the mating surface or in the #5 or 6 intake chambers. The port cap just below and ahead of this bolt is soft and not leaking.
Could there be a crack at the bottom of the bolt hole?
After the leak started, I made sure all the manifold bolts/nuts are torqued correctly and they all were but the leak persisted.
Before I go forward with pulling the head to have it looked at, any guesses as to where else to look?
Thanks for taking the time!
My upper radiator hose popped off and dumped coolant. Engine temp needle went to about 1/4” from the lower edge of red on the gauge for about 30-60sec before I cut the engine off.
Engine has run fine since - for about 10 days since losing coolant - but developed a coolant leak (no evidence of oil & coolant mixing) with the strongest flow while cooling down. It would leave a small puddle about 6” across over the course of 20-30minutes after turning the engine off.
I tracked the leak to the second to last lower intake manifold bolt so I pulled the manifold today expecting to see a crack in the head but it’s not showing anything that would produce a leak, at least not on the mating surface or in the #5 or 6 intake chambers. The port cap just below and ahead of this bolt is soft and not leaking.
Could there be a crack at the bottom of the bolt hole?
After the leak started, I made sure all the manifold bolts/nuts are torqued correctly and they all were but the leak persisted.
Before I go forward with pulling the head to have it looked at, any guesses as to where else to look?
Thanks for taking the time!