My Turd

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Joined
Dec 15, 2007
Threads
202
Messages
2,713
Location
North Bend, OR
Well My 62 that I sold got some love tonight. (Sellers remorse) Its new owner will be traveling with us tomorrow morning to Uwharrie for the day. As many of you know the exhuast was horrible and it ran HORRIBLE....wouldn't start on cold days or when ever it felt like it.

Well Venessa, the new owner, brought it over and we at least started a fairly good tune up. She had new exhaust put on it (Darin...those guys you recommended did a shotty job...I'm going to tell her to bring it back probably) and they were able to tighten the pully on the belts that I could not get to budge.

As far ast the tune up that was fun. She was not able to get a Dist cap and rotor in town. Well we went to dive in and am surprised this thing ran at all. The main power plug from the coil could not have been touching any metal what so ever. The plastic was cracked and the entire plug was covered in some oxidization. Looked like it was filled with silicone. Amazing. So we found a store up in Sanford that had a cap and rotor and picked it up with a new headlight that was out.

Anyway...new plugs, wires, rotor, cap, air filter, oil change, light and the thing is a new car. No $it went from zero to 60 up hill in like 12 seconds. I don't think it could go from zero to 60 ever before. Power all thruout the band where before you got nothing below 2.7K RPM.

Anyway she has been on this website a lot and I'm sure she will read this but she will be there tomorrow to test out her skills on the trails. I think she will be our first Female Owner/Operator in the club.
 
Was that you/her behind my house in the sand pit? I could tell it was an SUV in the dark but wasnt positive.

See you at 0730.
 
Kens muffler did a shooty job ? You need to go back and talk to Ken himself then . Ken will make it right. I hope Mike is the one that did it for her. Please ask her if it was ? Or i will this morning. That makes me a little upset now because i recommended that place. I have never had a bit of problem there before what soever.
 
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Kens muffler did a shooty job ? You need to go back and talk to Ken himself then . Ken will make it right. I hope Mike is the one that did it for her. Please ask her if it was ? Or i will this morning. That makes me a little upset now because i recommended that place. I have never had a bit of problem there before what soever.

Hey Darin,

Yeah I will ask her this morning and I'll have you check it out to make sure I'm not just not getting to picky. I should have probably explained a little better to her what should have probably been done. They left a lot of the old exhaust on there that is rusted out and didn't change the routing (thru the spring and still hanging way under the frame where it can get hit). that and they didn't move the 02 sensor locations (one of them is broke on there and it is very obvious why it is broke as you can not get a new one in as it is up against the transmission.

As far as a lift she was ready for some new tires and I'm going to talk her into probably doing some Long AALs and the lift shackles I have in my garage and some 33s. Now with all this new found power, at least 100% more, it will spin those 33's no problem now. Sure beats the 28's that are rolling on it even though those are brand new tires.

Yes that was me over there. I was making sure she new how to engage the 4WD and Low Range. But it appears that my H4 stopped working. I'm told that it rarely works when people get the rigs but mine did when I had it a few weeks ago. I'm thinking maybe the vaccume line got hit and disconnected.
 
Jason, could also be the vaccum on the firewall, those are common for going bad on the 62's. Let me know if you want to look into this and I will assist.
 
Jason, could also be the vaccum on the firewall, those are common for going bad on the 62's. Let me know if you want to look into this and I will assist.

It was intermitant this weekend but finally after a big bump on the trail the light clicked on and it seemed to be working again. Not sure if it is the Selenoid underneith or a lose hose
 
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