First post but I’ve been lurking for a while. I was doing the injector washers today and uncovered a nasty little surprise on my ‘91. The bolt wasn’t in there too well and half the pedestal was broken off.
I noticed there was lots of material left on the head, so I drilled and tapped the bolt hole deeper, and installed a longer bolt through the hold down. It torqued properly with the other ones.
Basically looking for some opinions on the fix. I took a feeler gauge to the other hold downs and it seems the hold down doesn’t actually make contact with the pedestal, but rather engages the dimple on one end, and the injector body on the other. I was able to tap almost a full centimetre so the bolt has plenty of bite in the head.
I realize the proper fix is to replace the head or at least take it to a machine shop to see if they can weld it up, but that would be a shame, as the engine is very new, and time is rather limited at the moment