Took the LX for state inspection and the garage told me I had a significant fuel leak from the #1 injector ...

I have no sense of smell (not Covid related) and could not smell the fuel, but could see it streaming out once I knew where to look. Lesson learned, if you do your head gasket and notice the truck taking longer than normal to start while cranking it, start looking for a fuel leak.
An entire head gasket re-build taken down by this ...
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Disassembled everything needed to replace the o-ring, luckily I saved the old ones as just in case. Took me 2.5 hours to get the washers and banjo bolt back into the fuel filter, such a tight fit from up top and I don't know whose arms could fit in from the wheel well or what knuckle dragger can reach it from their back underneath either.
Once the upper plenum was back on the hard part is over and goes quickly ... except when you accidentally pull off the 12mm socket from the extension when tightening the lower throttle body bolts and the socket disappears into the abyss and doesn't hit the floor. Took the TB back off and looked for it from all angles ... GONE. It belongs to the truck now. I will let it keep it as a trophy for surviving the repair process.
Just got the call now that it is done and passed inspection now. It's been down almost a year for repairs. Hoping it lasts a good long time again now