Just got back from a successful trip to Coal Mine Cruiser Classic in PA. After getting that low voltage issue sorted on Wednesday night, we were ready to hit the road on Thursday morning. Before leaving I checked most of my nuts and bolts to make sure nothing had come loose, all good. I checked my fluids, all good.
On the cruise out, I was putting the motor through it's paces, there are many long grades, some steep along our planned route. I pushed the motor up to 28lbs boost, the max EGT I saw was 1150 doing about 80 mph up a long grade with a fully loaded rig, towing a fully loaded M416 trailer.
Everything was going swimmingly until I crested the last of the big passes, as I am coasting down the backside of the mountain, it starts raining, very localised rain, its just hitting my windshield...cr@p that's my coolant spraying.
I pull over and investigate, my radiator cap is missing, nothing is leaking or broken. I didn't fully secure the cap before leaving in the morning after my fluid check. I fortunately found the cap in my auxiliary battery tray. I fill up the radiator with water I was carrying (about 9 liters was needed), and then continue on to camp without issue.
Cute cabin, the wifey approves.
The next morning I miss my alarm, wake up in time to race out the door and drive 45 mins to Anthracite to meet up with the guys
That left an hour earlier. I spend the day running black Diamond trails with a group of heavily modified 40's...that's one heck of a way to break in a brand new drivetrain.
The granny low 1st gear is such an improvement on the crawl ratio of the stock setup, I can only imagine how it's going to be when I get the marlin gears installed.
Towards the end of the day, crawling down a particular steep (think flip forwards steep) hill, I hear a binding clunking noise twice. We stop to investigate and can only replicate it when the front hubs are locked. As we are on our way out I figure I will diagnose the issue later.
On the last hill decent I picked up a sizable log that jammed between rear axle, frame and body. Luckily one of the guys had a folding saw which made fairly quick work of cutting it out. The bad news is that log took out my rear airlocker airline, again I will fix that later.
I put it in RWD and head back to camp about 50mins of up and down mountain passes, lots of switchback etc. definitely giving the motor a good workout.
I pull into my cabin, turn off the motor and hear a hissing sound...dear God now what. Open the hood and see I have steam spewing out of the bypass nipple on the radiator, the same one that I had cut down and glued a screw into.
The water that I had put in the radiator the day before had boiled, built up enough pressure to pop the weakest link, I am lucky it was just that screw. I JB weld the nipple hole and left it to cure overnight.
Next morning I drain out the rest of the water (it was still mostly full) fill up with coolant, that @fireball had graciously procurred for me, test drove it for about 30 mins, all is good, it holds and I'm good to go. We enjoy the rest of the festivities, won a bunch of cool stuff at the dinner raffle, burn the candle with good friends, new and old, and then pack it in for the night by 2am.
After breakfast on the deck this morning we loaded up the Cruiser, trailer, dogs and family and headed for home, no issues to report on this last leg of our first adventure.
As I arrived in my town, I didn't need to fill up the tank yet, but I did so that I could calculate the MPG. I had to do some additional math to figure out the true mileage since I have not yet calibrated the speedo to account for 4.56 gears and 37" tires. Unless I screwed up the math, looks like I got 22.9 mpg over the 457 miles I drove this weekend. This is far better than I expected, especially given the spirited driving I was doing, all the mountain passes with a loaded trailer and the day of crawling I did. Pretty stoked with the performance and mileage.
I am claiming adventure #1 a success.