So I had the leak down test performed.
The mechanic said, they heard air escaping from the crankcase. They added some oil to the #4 Cylinder and now the Compression is now at 177 psi from its original test of 170...
They basically said that its an internal issue(long block) and that the rings are worn, and would recommend an engine replacement if I want to fix it. What are y'all thoughts on this? This is out my level of expertise so I'm not sure where to proceed
I wont do it.