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- #221
I got another big job knocked off my to-do list yesterday, and pulled off the intake manifold, cleaned it and the crossover pipe, and resealed everything with fresh OEM gaskets. I'd been seeing an oily buildup around the IM to head seals, so I assumed it would be disgusting in there, and that I may be losing air at those joints as well.
This involved removing the crossover pipe, removing the PS reservoir from the IM, along with the oil and trans dipsticks, throttle bracket, injector lines from the injectors and the injection pump, the fuel return rail and hose to the IP (don't lose the copper seals, there's one on top and bottom of the fuel return rail, use new when reassembling), some wiring to a sensor on the IM, boost reference to the boost compensator from the crossover pipe T, a wiring connector attached to the throttle bracket, and finally pulling the IM and injection lines out of there. It was a near full day job working at my pace, about 6 hrs start to finish.
Observation #1: about 2/3 of the IM bolts were loose! As in, no torque to break to loosen them, finger tight! So it makes sense I was seeing oil buildup, and it would make sense if I was seeing air escape there at higher boost as well.
Observation #2: it was much cleaner inside than I expected, no gunky buildup in the IM or crossover tube, a bit on the back face of the valves you could see down the runners, but not what I was expecting at all. This really cut down on how long I thought this job was going to take, I had planned on taking them somewhere to run them through a parts cleaner, but that was unnecessary.
Pro-tip: I ziptied the injector lines to keep them in the same spot/order as when installed, as you need to remove 3 of the clamps that keep them in order to get at the bolts for the IM, made it much easier to figure out where everything went back to when it came time to reassemble. The injector lines came out with, and stayed with the IM.
While I was in there I pulled the valve cover off and bent the flaps further closed to reduce the amount of oil that makes it into the vent hose from flinging off the valvetrain. No idea if this will help or not, but I can't see how it could hurt, there's still lots of gap for air to move freely through.
Results: butt dyno feels there could be a small increase in power and responsiveness, but it's small, and could be made up.
Now it's time to play with tuning!
This involved removing the crossover pipe, removing the PS reservoir from the IM, along with the oil and trans dipsticks, throttle bracket, injector lines from the injectors and the injection pump, the fuel return rail and hose to the IP (don't lose the copper seals, there's one on top and bottom of the fuel return rail, use new when reassembling), some wiring to a sensor on the IM, boost reference to the boost compensator from the crossover pipe T, a wiring connector attached to the throttle bracket, and finally pulling the IM and injection lines out of there. It was a near full day job working at my pace, about 6 hrs start to finish.
Observation #1: about 2/3 of the IM bolts were loose! As in, no torque to break to loosen them, finger tight! So it makes sense I was seeing oil buildup, and it would make sense if I was seeing air escape there at higher boost as well.
Observation #2: it was much cleaner inside than I expected, no gunky buildup in the IM or crossover tube, a bit on the back face of the valves you could see down the runners, but not what I was expecting at all. This really cut down on how long I thought this job was going to take, I had planned on taking them somewhere to run them through a parts cleaner, but that was unnecessary.
Pro-tip: I ziptied the injector lines to keep them in the same spot/order as when installed, as you need to remove 3 of the clamps that keep them in order to get at the bolts for the IM, made it much easier to figure out where everything went back to when it came time to reassemble. The injector lines came out with, and stayed with the IM.
While I was in there I pulled the valve cover off and bent the flaps further closed to reduce the amount of oil that makes it into the vent hose from flinging off the valvetrain. No idea if this will help or not, but I can't see how it could hurt, there's still lots of gap for air to move freely through.
Results: butt dyno feels there could be a small increase in power and responsiveness, but it's small, and could be made up.
Now it's time to play with tuning!